From traditional coal-fired boilers and oil-fired boilers to the heating source of the drying room, to the full-automatic computer-controlled automatic temperature control and control of the “energy saving and environmental protection automatic control drying equipmentâ€, Liu Dachao invested more than RMB 10 million in relatively backward boilers in the tea processing industry. The drying room has been upgraded and upgraded to increase production by 30%, while saving more than 3 million yuan in fuel costs a year.
Recently, it was learned from Yunnan Liuda Chashan Tea Co., Ltd. (hereafter referred to as Liuda Chashan) that, after more than one year of experimentation, the “energy saving and environmental protection automatic control drying equipment†developed by the company has been fully put into use. The measurement data shows that the new self-controlled drying equipment has increased production by 30% compared with the traditional boiler drying room, and the entire process automatically controls the temperature and controls the time, zero pollution and zero pollution, and truly achieve green drying.
“In May and June this year, 10 sets of equipment were built, all of which were put into Linyi Fengqing Pu'er Tea Processing Base. The effect was very good. Not only did it reduce energy consumption by 65%, but also the annual drying capacity of Pu'er tea was 2000-2500 tons. It has grown to 3,000-3,500 tons, and the fuel cost for one year has also saved more than 3 million yuan." Talking about the self-developed "energy-saving and environmental-protection-controlled drying equipment", Yang Jun, the deputy general manager of the six major Dasan Hills, is very proud.
Recently, it was learned from Yunnan Liuda Chashan Tea Co., Ltd. (hereafter referred to as Liuda Chashan) that, after more than one year of experimentation, the “energy saving and environmental protection automatic control drying equipment†developed by the company has been fully put into use. The measurement data shows that the new self-controlled drying equipment has increased production by 30% compared with the traditional boiler drying room, and the entire process automatically controls the temperature and controls the time, zero pollution and zero pollution, and truly achieve green drying.
“In May and June this year, 10 sets of equipment were built, all of which were put into Linyi Fengqing Pu'er Tea Processing Base. The effect was very good. Not only did it reduce energy consumption by 65%, but also the annual drying capacity of Pu'er tea was 2000-2500 tons. It has grown to 3,000-3,500 tons, and the fuel cost for one year has also saved more than 3 million yuan." Talking about the self-developed "energy-saving and environmental-protection-controlled drying equipment", Yang Jun, the deputy general manager of the six major Dasan Hills, is very proud.
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